Karl Wingett-Smith remembers activities that were going on
concurrently with those in his earlier article….
The Installations Department (ID) office was in a
corner of the
Experimental Shop at the river end of the Kingston site, beside us was
the Structures Department and, in the more palatial area upstairs, was
the Advanced Project Group.
Within the main Experimental building, were two ID facilities: the Electrical section under Ron Leader and the Hydraulics test rigs that were under Hamish Waugh. I never knew exactly what Ron & Co got up to (electrics are not exactly my forte, things aren’t live unless you get a big flash and bang when you join two wires); Hydraulics had two interesting rigs, though. One of these we all called Cloche Merle, due to its resemblance to the traditional Paris street urinal (a circular screen with a gutter and drain running around the inside somewhat below waist height. The virtue of that was that it enabled a gentleman relieving himself to raise his hat to a passing lady.) Despite my digression, that was ID’s centrifugal test rig whereon fuel or hydraulic components were attached to a rotating arm while the gutter caught any escaping fluids.
The other was a wooden chair with a control column
set up in front of it which, when connected to another, more complex,
set of odds and ends (Derek Holden or someone else may be able to add
more detail to this) created a hover flight simulator. Anyone,
primarily the test pilots, would sit in that seat and try to keep the
represented aircraft stable. Beyond the fact that, obviously, the
pilots coped fine (as did Hamish who, I understood, flew Avro Ansons
during WW2) while I, with a current PPL, failed miserably during the
one go I scrounged on it.
When I first joined HAL the six P.1127s were under
construction there. When they went to Dunsfold for final assembly their
space was taken by a substantial number of Hunters that had been
replaced in the RAF first line interceptor role by the new Lightning.
The Hunters were mainly being completely refurbished to become the Mk
66 for export to India, while a few became two seat trainer variants.
Fuselages and wings were trestled separately.
When contractors were working on the roof and a fire was discovered
there during their (and our) lunch break the Fire Brigade and Salvage
Crews were called from their base just across Richmond Road. They
arrived about 15 minutes after the alarm was raised! The fire crews
played water on the roof and that brought down chunks of smouldering
insulation that fell inside the shop, some of it landing on wings, more
falling inside the open cockpits from which canopies and seats had been
removed. Naturally a fireman’s instinct is to pour water on anything
that might flare up and this involved turning their hoses inside the
cockpits. Those of us who were in the building decided that this really
wasn’t the best idea and grabbed CO2 extinguishers and waited
underneath the wings so that we could use that and prevent water
damage.
Also in the Experimental Shop was the Hunter Fatigue
Test Rig in which some poor airframe creaked and groaned to its final
destruction that occurred with a very loud bang ‘when something broke’
to be followed by the clatter of all the shackled weights used to
simulate flight loads. Not exactly a quiet life, but more about noises
later.
Cockpit pressure testing was also carried in the
Experimental Shop. A large rectangular tank, rather like a swimming
pool, had been sunk into the hangar floor, lined with white tiles and a
guard rail placed all round; it was something like six feet deep and
had a gimbal mounting at each end. A P.1127 cockpit was mounted on
these, the pool was filled with water and the cockpit pressurised. The
canopy protruded slightly above the water level so that it could be
pushed to roll the cockpit section over to examine the underside etc. A
good idea but it proved more difficult to turn over than expected. The
shop foreman at that time was one Charlie(?) Price who had a reputation
for never asking anyone to do what he wouldn’t do himself. Rumour at
the time was that he had been involved in undercarriage retraction
testing on a Fury and been picked up by the tailwheel; a larger man
might have suffered severe injury. Anyway, he climbed over the safety
rail and, using a long pole, leaned hard on it to push the cockpit
over. Whether the pole slipped or the cockpit moved suddenly I don’t
know; all I saw was that he fell into the tank. He emerged out the
other side and I’ll swear that he was bone dry above the knees. I am
convinced that he included walking on water as just one of his
capabilities.
The Robin Hangar across the yard held more of the ID
test facilities: the air conditioning rig, the reaction control nozzle
rig and the hover rig. Here the prime members of staff were Stan
Williams, John Davey, Roger Samways, Tony Harris and Dave Tait, the
last being our own fitter who could usually find ways of adapting these
rigs for their various specific uses.
Unofficially, certain ‘foreigners’ were made there. For example, a
very simple bit of tin bashing created a ‘hole’ with a lead-in ramp all
round that enabled us to practice short range putting on an otherwise
level floor. Also, having broken a half-shaft on my Rochdale-Ford
Special for the third time as I arrived in our adjacent car park one
morning, it afforded me the opportunity to change the complete axle
assembly. I found a fractured casing that had been missed by the two
garages who had replaced the previous ones. The shaft that I removed
showed evidence of fatigue, caused by flexing with every rotation. That
old axle may have been discovered when the site was redeveloped and
builders excavated for the foundations, otherwise its likely to be
still buried there for posterity.
Most of these test rigs individually created a lot
of NOISE! Also, even though we were literally next door to the
Compressor House (run by Fred) with several large, 200 psi receivers
between us, there was generally only enough air to run one of these
rigs at a time. Inside our little hangar were several heater units
connected in series so that we could get air at temperatures
approaching 400 C and at 200 psi. These weren’t shielded in anyway,
apart from insulation jackets. We became a bit concerned when some of
the Tungum pipework showed evidence of wall thickness reduction due to
corrosion beneath these blankets.
Now to the tasks undertaken there. In an earlier
article I mentioned our cockpit air conditioning rig, an almost
complete P.1127 fuselage section between front and rear pressure
bulkheads with the entire system in its expected locations in the real
aircraft. Cooling air for the heat exchangers was ducted into them from
a large fan to simulate flight and ground air flows. The cold air unit
could be run up to its maximum speed of some 66,000 rpm and all engine
bleed air (up to 200 psi) came via the heaters mentioned above. We
required, I think, a hot air flow variable up to 18 lb/min regulated by
our own design of pressure regulating and flow control valve. This
consisted of a fixed orifice plate with a precisely shaped ‘carrot’
moving along its axis to vary the area of the flow control annulus. We
did all the calculations on this and it was manufactured in-house by
profile grinding. John and I used to set these up, matching carrots,
orifice plates and springs on the rig to match the theoretical
performance we sought. This could be pretty noisy with the in-cockpit
levels exceeding 95 db. Mind you, at that time, nobody had begun to
challenge the long-term damage caused by this; I am now totally deaf in
one ear (but I also did a lot of small-bore rifle shooting…)
Although John and I could make a lot of noise it was
(in my opinion) much worse when Roger Samways was testing the reaction
control or ‘puffer’ nozzles. These not only required flows of very hot
air at 5 lb/sec to be released as quickly as the valves could be opened
and closed (to demonstrate and prove effective sealing and component
life) but he also used to sing at the same time!
The other major cause of noise was the hover rig.
This was a Dexion frame on which was mounted a black-painted ground
board that could be adjusted for height and angle in X and Y axes with
a scale model of the P.1127, complete with engine nozzles, fixed above
it. This enabled simulated hovers at variable heights and attitudes
relative to the ground. In itself it made no noise….until the air
supplies were in use. The ‘fan’ or low pressure compressor air for the
front engine nozzles came from our communal 200 psi supply and heaters,
whilst the rear high pressure compressor ‘hot’ engine nozzles, were fed
from the noisiest source of all, a Bristol Proteus turboprop engine
combustion chamber (or can) that was fired up with its exhaust pointing
either outside the hangar or through the rear nozzles on the model.
Engine intake suction was represented by something else (I don’t know
what!) Anyway, the can was so loud that nearby householders lodge
complaints and a silencing system had to be devised and installed.
Before running the hover rig, the black ground board
was coated with an emulsion of white titanium dioxide in oil to show
air flow paths as the engine nozzle exhaust hit the black ground board
and potential re-ingestion of engine nozzle air by the engine. Any
significant volume of hot air reduces the engine mass flow and,
consequently, the thrust produced. It was on this rig that under
fuselage strakes were tested and developed.
You have to remember that all this took place
between April 1960 and September 1962 when private car ownership was in
its infancy. I mentioned John Apted’s Hillman Husky earlier; that was
the only car in which I have ridden that was equipped with a four point
seat harnesses. Ray Searle had a reverse sloping rear-window Ford
Anglia 105 E, I had a former Fordson milk delivery van with much
modified chassis, suspension and a Rochdale Motor Panels and
Engineering GT bodyshell. In shape this was not unlike an E Type Jaguar
that hadn’t yet been produced - there the resemblance ended. Stan
Williams had a Morris Minor, a new model, not a 1930’s two seater of
which Roger was so proud!
We all used to park alongside the ID Robin Hangar
where there were both a hedge and a ditch. One day Roger had a trade
visitor who was taking him out to lunch, they were going in Roger’s
pride and joy. His colleagues had other ideas, however. The fabric hood
had only a very small rear window and Roger had parked nose to ditch
and hedge. Ready to pop out for lunch he climbed aboard, started up,
engaged reverse and moved slowly forward, slipping gently into the
shallow ditch despite increased revs. Unknown to him, three of us were
bent double behind lifting the rear wheels off the ground and pushing
slowly. Of course it was easy enough to extract him! So, you see, the
mixture of work, learning and (a little) fun created a pretty good
atmosphere and some friendships that have stood the test of time.
Another task with which I was involved was a study
of kinetic heating and heat transfer, where I was led by Rene LeClaire.
This was in the context of the supersonic P.1154 that was anticipated
to be capable of protracted flight at Mach 1.7 (while the fuel lasted)
and up to 15 minutes dash at up to M 2.3. This latter was limited by
water spray injection into a water boiler to cool the air through the
air conditioning system heat exchangers. I did the sums on that and on
the weight vs performance balance for cockpit insulation. René did the
bulk of the theory on cabin heat loads and between us we devised an
approximate method of calculation.
We concluded that the nose of a
single seat aircraft could be represented by a cone and that the pilot
and equipment inside by a frustum of smaller diameter. The space
between was the path of cooling air. We produced a report on this (I
still have a copy) and designed an electrically heated specimen for
tests. Having done that I moved on for the reasons given in my earlier
article and missed that work. Since the next government axed the P1154
I have no idea if our work on that was ever of any real value. Does
anyone out there know?